Alright, got the photos up. Here we go!

taking off the 40mm fan

the grating isn't built in, but it is aluminum. looks good too, it's powder coated or something cause it's not smooth.

unfortunately part of the casing is cracked, since the soldering of the wires was sticking up a little bit more than it was supposed to, thus increasing the diameter and cracking the plastic when it was pushed down. no biggie.

decals went straight to my netbook :mrgreen:

a look on the inside of the ESC, from the battery end

underneath the battery end. I think they used thermal adhesive on the BEC coil to stick on the end cap, but it doesn't adhere very well to the plastic.

capacitors are on the motor end of the ESC as well. black gunk to keep it from detaching.

it could very easily be run PSU style with a fan creating airflow through the ESC

gigantic 8AWG beefiness.

I sure am glad I have my reflow station because with just a 45W iron these would've been impossible to solder. 500W of 400C air was enough to melt all of the solder and form a good connection on all of the 6.5mm bullets.

okay, now how am I gonna do this...

there's some aluminum dust from the slipper but not as much as I thought. It's still working perfectly, I'm very happy.

I had planned on changing the 1717 bearings out with the ceramic set I got from Boca...

really beefy looking.

front endcap taken off, bearing is just pressed in.

a closeup, a couple of whacks with a screwdriver and it popped out.

this was a disappointment though...the Boca set was 6x16x5. after googling a bit I found the correct size is actually 6x17x6. Just in case though, I emailed Castle to confirm. I will have to return these and buy the correct sizes :?

while I was at it, I replaced the RS4 dogbone in the front of the E-Revo.

the TC5 bone blades were pretty wrecked though.

at least it's still in one piece and not bent this time.

no damage at all in the diff input cup, RC Monster Mike knows what he's doing. (:

more metal dust, this time it's from the dogbone. there was damage of some sort on one of the balls, dunno how it happened but there you are...

the bone blades survived, more or less, but they are unusable.

the 6mm dogbone was indeed too small for the job. it was overtaxed by the job of the front center driveshaft...the front was usually off the ground when accelerating, but under braking the full force of the truck overwhelmed it. This is proven by the direction of the twist, which is clockwise (power from the transmission is clockwise, which would result in a counterclockwise twist).

size comparison of the new 7mm dogbone. I would've preferred an 8 but that's all I could find... the damage on the old dogbone is visible on the right side.

taking the washers out of the transmission to lower CoG back down to stock height. the mesh of the gears I'm using (24/54 0.8M) is big enough to clear the shaved rear shock tower.

checking the wear on the rear center driveshaft. RCM drive cup slightly affected.

Traxxas drive cup not so good...

Traxxas drive cup slightly dimpled from the front center driveshaft

new driveshaft in. Only about 2mm front/rear play with the cups.

a shot of the motor mount post mod. It's hard to see cause the washer is mostly poking out the back, but the lip of the washer goes over the motor mount, thus removing any play on it. It's a lot stronger and stiffer than just having the gear mesh screw at the top.

heatshrinking the bullets. It looks creepy, lol.

drilled a 5/64" hole, to tightly accept an M3 screw

having fun heatshrinking the Mamba Monster motor terminals

looks like a very clean install to me. two layers of sticky foam underneath (directly on the heatsink...not my ideal solution but it works) and a screw in the location I drilled earlier. I was also able to run the receiver cable through the heatsink fins, I doubt it will cause problems.

top view of the setup

you can kinda sorta not really see the screw, I used the last button head M3x6 stainless screw from my TC5R set.

I had to cut out nearly all of the rear left battery vent for clearance, the capacitors are huge! the spaghetti in there is my balance tap :mrgreen:

looking from the rear

can't put a fan there anymore, not without a Y adapter anyway. Used the bracket for some wire management.

data log from my run in the video. I could hardly break 2hp on the damp road. I took it out again this afternoon on some dry grass so we'll see how much power this baby's dumping! I actually ripped off one of my tires, I will need to reglue it...

very happy with this setup.
I will also be reusing the Losi Zombie-Max tires, I glued them to some RPM Revolver 3.2" 17mm rims last night. I am trying a new idea on the stock Traxxas foams, using spray adhesive to stick the ends together.

despite being dirty and dusty, the adhesive works pretty well. I used some 3M general purpose SA that I had laying around.

it becomes extremely tacky within two minutes of spraying on, I can only imagine how strong it is when it's fully cured.
Here's the log from my run this afternoon on grass:

I also glued on the Zombie-Max tires to the Revolvers, I'll see how those do tomorrow.
Also rethinking my cooling solution.

this will do for now, but I would like to try getting both the ESC and motor with a single fan.

tearing down the slipper clutch

inspection...not too bad, actually. I expected the hub slipper plate to take more damage than the spur slipper plate, but it seems fine.

went legit - Hot Racing long aluminum slipper pads

they machined the holes big, so I used some loctite to temporarily stick the pads to the spur assembly

install complete